| | Re: Patched firmware to improve rotation sensor, was Re: Robolab, byte codes and assembler Dick Swan
| | | "Philippe Hurbain" <philohome@free.fr> wrote in message news:Hp4JAs.oK8@lugnet.com... (...) Much to my embarassment, I have to agree with Philippe that the patch doesn't work very well. I try to figure out what went wrong. (...) This is the expected (...) (21 years ago, 29-Nov-03, to lugnet.robotics, lugnet.robotics.rcx.robolab)
| | | | | | | | Re: Patched firmware to improve rotation sensor, was Re: Robolab, byte codes and assembler Don Stauffer
| | | | | (...) Doesn't that mean that at any given count, you could still be off by 1, but now the odds of having an incorrect count are 50-50 instead of about one in 500? (...) There has been some discussion about whether this patch will work with Robolab, (...) (21 years ago, 30-Nov-03, to lugnet.robotics, lugnet.robotics.rcx.robolab)
| | | | | | | | | | Re: Patched firmware to improve rotation sensor, was Re: Robolab, byte codes and assembler Philippe Hurbain
| | | | | (...) It took me some time to figure out why, but you are right, the ambiguous transitions occur only while counting up. What you could do though would be to count +1 while going from state3 to state2_ambiguous, and correct "phantom transition" by (...) (21 years ago, 30-Nov-03, to lugnet.robotics, lugnet.robotics.rcx.robolab)
| | | | | | |